Ok first off, sorry my profile ans signature are misleading and i left out lots of information (I will shortly change that). Second im only 20 years old enrolled full time in an Automotive Technicians program so most of my time is spent studying for my ASE's so most of my time and attention is devoted there. Here's the story, i found the 74.5 260z at my grandmas house last year and me having mo car decided to restore it and use it as my daily driven vehicle. The motor was orginal, P30/E88, garbage smog control carbs n36 manifolds. My father being stubborn would not let me junk them for original S.U., triple mikuni, or webers. I spent weeks fighting those dreaded flat tops. The best i could get was an idle at 900 and a drive that was less than pleasant. After much debate he gave in and decided that it was not the most effective fuel delivery system. He opted for the clifford/holley kit. Yes i know that money couldve been spent on triple mikuni or nice rebuilt pair of S.U.s but being the muscle head he is i settled for that, i wont argue with someone whos willing to spend that kind of money for me. So that was that and the car was now operable, but not legally. While i waited to save money for registration and several months of insurance, i stripped the car inside and out, sanded her down and primered , cleaned up the wiring, bought recaro specialists, and MSA victory spoiler and front air dam with cooling ducts.
Heres where it gets interesting;
I decided to overhaul all my gaskets, so i pulled the motor (p30) disassembled it and replaced what was given to me in the gasket overhaul set including valve stem seals. Heres where i foolishly did not think AT ALL. I replaced one of the smaller water pump bolts with a new one from a assorted set of fasteners i ordered from eBay from a private seller. Upon doing this i broke of a piece of the block casting, creating a time bomb. I had no knowledge of this and when i was ready to turn on the car, i turned the ignition and was only greeted with spinning of the starter. I could tell that no compression was being created so i did a compression test and lost all compression in all cylinders. This is where i pulled this motor and started looking for another one
Part 2
Down the street was a 79 280zx sitting because it could not pass smog one year due to a fault in the smog system. When i popped the hood i.could clearly see wiring performed by someone who.clearly did not have any.experience just some.extra wire and electrical tape. This is the motor i pulled, junked the fuel delivery, well i still plan on using the EFI manifold for turbo, but cleaned this motor up, used ORIGINAL fasteners, new gaskets and blah blah. I pulled the 5 speed from the ZX as well.So now this is where i stand. A 74.5 260z with a 79 N42 block with n47 head. Sorry for the novel but hopefully this cleared it all up.
Thank you for the info, it really has cleared up my question, next time i will be sure to post adequate information