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motorsci

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Posts posted by motorsci

  1. I read the topic That dragon fly started maybe iam simple but my plan was to measure the before and after valve train weight and figure the difference as a % then subtract that from the valve spring tension and order springs 

  2. I read the topic That dragon fly started maybe iam simple but my plan was to measure the before and after valve train weight and figure the difference as a % then subtract that from the valve spring tension and order springs 

  3. Thank you all for your input I have titanium retainers locks and DSI valves from Datsun spirt I have a good unmolested. Set of rockers to put in but just enjoying a little time off work and waiting for the machine shop have a press with a tension gauge and was going to make a fixture to measure the deflection at the tip and what it takes to break it compared to a stock rocker here is a pic it ready to polish 66 grams 

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  4. If you think its detonation get some copper tubing and a cheep stethoscope from harbor freight pound one end of the copper tube flat and drill a hole in it bolt it on the motor close to the head were the heater hose runs is good run the tube into the car and hook up the stethoscope hose to the tube if you here detonation you know its timing if you don't a least you wont be guessing there are electronic versions of this that I own but I still use this for tuning 

  5. I should also mention that budget cuts have forced me to be creative with my class 2 hoard this is a stock 240z bottom with a p90 head and notched block for valve clearance.  with a 280zx cam and a 280zx turbo oil pump I know it wont make as much power as a 280 turbo but its what I have  and Iam sure it will be fun until the next motor. That beaning said this is very well put together hobo motor most of the time this sort of thing starts with 2 cubes of Key stone this was a clean build 

  6. The center section was replaced when it was rebuilt the compressor wheel has ate something in a previous life but was there before the rebuild I asked about replacing the wheel the re builder said it was fine  

  7. the failure is that its pushing oil out both ends of the turbo the feed line is also new 

    the in line filter has no restriction I ran this setup on my old motor with no issue the car made 65 psi oil pressure on startup as always 

  8. I just got my draw through turbo back from rebuild new motor this happened less than a minute after start up the burning oil forced me to shut it off. The turbo was pre oiled  the drain is clear and perfect low crank case pressure as well.  The turbo failed from my last engine coming from together and debris. This time it has a in line filter wih no restricter its a journal bearing rotomaster (Garrett T04 ). Has any one ran in to this I want to make sure I've checked every thing before returning it to the rebuilder

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  9. Thanks for the complement this is my first roll cage. but it does apper to be a total loss your right the main hoop is more than 180 degrees so out it comes. I am looking forward to making my gusets I juist got a 1inch demple die.

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