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Spdrcr

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Posts posted by Spdrcr

  1. OHMYGHERD! tranny woes continue. Checked the level and it was low so I added some more. Still was getting some air out of the dipstick but I thought it might have been from being low on fluid. What do I know about auto tranny? Nada. 

     

    anyway, took it out for another drive. Shifting much better.. and when I stopped at the end of the street...  poof! fluid goes everywhere. And I mean everywhere. All over the whole car, the paint all the way to the trunk, the window, the entire engine. The dipstick popped out from the pressure and  the fluid hit the rubber stopper and then bounced back. What a mess! 
    01888249-BF31-413B-8BBB-6C8EE35B0DE1.jpeg.ed61aaa7dcb80daf36dce59621871bc0.jpeg7F2CDC86-40D5-4713-9A32-2278CA7CD4E0.jpeg.e58bc7f38f3ec77ccbe2e1c11ae630fc.jpeg

    get the car home and park and after I shut down I can hear the pressure coming out of the tube. I pulled the stick out a bit and a bunch of air came out. Spent about 2 hours wiping everything down. 
     

    Figured it was one of these things
    1. Overfilled - I am struggling with reading level but seems low still 
    2. Vent clogged 
    3. Filter loose in pan - car was crashed after all
    4. Trans is just broke
     

    Figured I’d start with vent. Had to drop the tranny down to get to it. Pulled the hose off and it seemed fine. Little tube seemed fine. I ran some wire through to make sure. Then rerouted the line. Put everything back. 
     

    started it up and everything seems to work fine now. No more pressure out of the tube. So either the hose was kinked or the tube blocked. We have a bunch of snow here so no test drive till later. Please no more fluid everywhere!

  2. A few problems. 
     

    first the new radiator is leaking when under pressure. eBay... 

    then coolant was shooting out of the little air hole in the overflow tank. Like 3 feet up. That was fun. I believe it was just air since I’ve run it up and down in temp since then and it’s been OK. I may get a different style radiator with the in/out on the same side so the upper hose doesn’t have to cross over. 
     

    second is transmission. 
    level was fine when I put it in. Go to drive and nothing. No drivey drive. Check fluid and it was all gone. Figure it all ran into the converter and whatnot. I don’t know how long it’s been sitting. Ended up needing 6 quarts and is still a touch low. (I ran out)

     

    after the first drive fluid poured out of the dipstick after I parked. Like a lot. Everywhere. Had to start the car to empty the tube. Fluid level was the same maybe a touch lower seeing as how much was now on the engine. I drove it again yesterday and after parking  I could hear air squeezing out of the dipstick. I pulled it and got a little puff of air. Lucky no fountain this time. I have to check the vent. Maybe I squished it during install. 
     

    I just went around the block a couple of times but the transmission is slipping and mushy. Could be broke or could be the slightly low fluid. 
     

    third is shifter is still not here.
    Ordered one last month and about to cancel if it doesn’t ship soon. I have a rig set up to get me moving. 

  3. Need to get the cooling system hooked up so I can run it up to temp. 
     

    upper hose

    D2E1ABEE-6C83-4E84-BA0B-9E991190BF39.jpeg.2d9e435ff24d4b7ddc85b9d89e3286ae.jpeg
    Lower hose

    64F14BBF-255C-430E-A87F-BFC42C0A68A7.jpeg.f03389d40a4ae6d659c350fbdec594e7.jpeg
     

    Steam port cut into the upper hose

    DE5E9183-E6AC-405F-8C13-EC5F1E8DC048.jpeg.3cc248cf21d66657bcf818db172bc816.jpegA8252EB9-F247-4F1C-A56F-42F6DA6727AB.jpeg.3c72cdf172bacb76d2257493efccd433.jpeg

     

    needed to mount an overflow tank so I grabbed a universal job. 
    19A7951D-9A9D-4D8B-BB8A-284B061A1C27.jpeg.4a405874c4a85a47d2c261409c979a33.jpeg
     

    gonna try and get it on the existing bracket

     

    B29782F0-0561-411B-BA88-A767CD5D1BC7.jpeg.693837f8fefb835ffd8cab47bc89fb77.jpeg408E5039-2778-4685-8AAF-5E77E829AAFD.jpeg.717759faf79fc937e337e22134b0e00a.jpeg

     

    it came with a bracket that the holes lined up perfectly with the holes on the car 

     

    FE017F33-D4D5-416E-B23C-4A5E4F7F88DB.jpeg.21bc5930c26c4d0795a5a271ff92a2e4.jpeg8A1C5D2B-D65F-4963-8B3D-C984298140E6.jpeg.7820f23d081c6a258ec7cfd648626a19.jpeg

     

    gonna chop it 

    ABBEF5D6-1779-4D0D-8324-97B2E23B9EE4.jpeg.f324f922be8f4cf1aa9604836510e7bc.jpeg
     

    warned you my fabrication is subpar 

     

    46E17086-5DE4-40CE-8573-101380D47300.jpeg.03cbf77cf0f363510c2e2eee2fedd7e5.jpeg7E2987E7-3E6F-403F-B2D4-C2E1997A5A77.jpeg.7e082f2ae9706cc28906d3651e9b4d0e.jpeg

     

     

  4. I love wire loom so much! I wish I could do it for a living... bleh!

    7EE5A5DD-2C04-448B-AD59-428C78D1E84D.jpeg.3c30931282c854f44300ce6df90dc43a.jpeg

     

    plug wire is hitting the battery tray. I don’t know if I’m going to fix the plug or the tray. 
     

    3E4E096A-F5D9-4A31-B028-9600C647CA37.jpeg.f07b9a16fdf64b0069d1ab64be4cdcd2.jpeg

     

    new driveshaft has arrived. still have to test it. 
     

    2E21B008-D67D-4D72-8CCF-3AFA28A1D46E.jpeg.1510fa94dd8e65924f660a652bb7ee9c.jpeg

    picked up some plugs for all the extra ports

    E9D31ACA-8F25-4445-88EE-1C98639E3BCB.jpeg.4ec97e0b4b5cc80c1f1f66dde8627e0c.jpeg

     

    my pcv is going to be the factory line from the throttle body to the front passenger valve cover

    rear passenger side plugged 

    rear driver side has pcv valve in the cover itself 

    pcv valve to old evap selonoid port  

  5. Got the fuel line ran. I used nylon braided line. I used the old fuel p clips and cut half the rubber out of it. That made a good spot to run the fuel line. I left 2 holes in the mount and that holds the brake line and power line. I forgot to take a pic of that. I’m going to get a 90 fitting on the fuel rail to change the angle a bit cuz the line sits on the battery. 
    D814AEBB-B4AE-4019-B758-910DCEE0B55C.jpeg.fc8090ea819ba0edb23ba089381c8315.jpeg
     

    I’m going to be an electrician soon if I mess with wires anymore. Here is the harness laid out. I’m really glad I didn’t wrap it on the bench. I had to cut the 02 sensors out to get the where they made sense. 

     

    A8211E86-C648-4624-88D3-B7C95B7868BF.jpeg.cee90db830a8fdfb5510cece04e6f8c1.jpeg
     

    I created a new wire pulling tool. I can make extras if anyone wants in on a group buy or something. 
     

    676DB6A7-2DC8-413A-9EBA-94070695AFFA.jpeg.ac17e24ea9fdbf0e5db84f7271e31502.jpeg
     

    this is an absolute mess rights now but I really wanted the ecm in the car to keep the bay cleaner. I was able to pull the factory wiring through the firewall and strip all the old wires I don’t need anymore. The I slid the ecm connectors one at a time through the hole. 
     

    2ED54E75-FF06-43A3-97A5-A0170E169BA8.jpeg.3b03a13de3a778711d7a6ed38c0b4c05.jpeg

     

    here is my fusible link replacement. Just plain blade fuses that are powered directly from the starter line. I put on the 4 red and white wires that came from the links. 
     

    98C0B1AE-73A5-4B56-ACF8-92863F8C9F2E.jpeg.4d59879f94122d2702dd6445d424dd6f.jpeg

     

    then I made up a relay box. Using 5 relays and 6 fuses. 
     

    fan relay and fuse 

    fuel relay and fuse

    starter relay and fuse 

    ignition relay and 2 fuses split pass and driver side coils, inj, etc 

    brake signal relay which will receive power from the brake light and ground the ecm tcc signal 

     

    4A905C7C-3D84-40BD-93DE-057102E42597.jpeg.32d33e2beecfb3d66933661f289fb569.jpeg60A65984-2D84-44C6-8E4A-0D98743CA541.jpeg.f5e8afafd7b5c227c4d6f290fbe1ad03.jpeg

     

  6. Drilled some holes for the trans mount. Rivnuts are fun. 
    34B0576E-4F66-44F3-B4CF-0D18E26C0C9A.jpeg.04d157dee94c07e25b504d33848a72e8.jpeg

     

    mount in. It’s a tight fit. 
     

    D5D4C807-0CF5-40E1-A3A4-18B9C3DB2372.jpeg.012515b99cf7f4cdc83f63361ee4550d.jpeg4FF3F371-D689-4B74-A355-C4B12D071EBD.jpeg.dc0becae5e9e0ed1671bec151c18c7c0.jpeg

     

    unfortunately I ran into into clearance issues. Not totally unexpected. The fittings for the trans cooler lines were squished on the tunnel wall. I tried to hammer it after dropping the trans down but couldn’t get the leverage. Then shenanigans ensued when I dropped the trans too much and the engine slid back so the intake was stuck in the firewall. Took me a minute to figure that mess out. Good times. 
     

    Ended up having to pull everything most of the way out and mashed the passenger side tunnel right on the crease about 1” in. 
    65E21A1B-C94B-48FA-B5B5-46BAF28DC44F.jpeg.9b6449df91aec792af84e6313c052640.jpeg

    added some paint after all the banging. Then put it back in. 
     

    Test fit the driveshaft and it was short. After conferring with you guys decided it was too much and contacted JCI. They are taking care of me. 

    3B453579-F221-4D5F-981D-B46DF83DC450.jpeg.7a268fc780105b6b17799a1e53ef2cf7.jpeg

  7. All right time to stop playing around. Bad boy is going in! DB49131F-7897-4AAD-B610-FB55FAA0E50F.jpeg.df4c183d80f5dbabd65e6295c8eb5f84.jpeg98B43ECF-637D-4898-BF60-EFBDC84BC87D.jpeg.3c5d46db1dba08b5bed8617ccd0793c9.jpeg9E17FDFA-6EF2-4C2F-AF0C-0B7142EAE2C7.jpeg.09372c5ae083201c9003c56b6f678451.jpeg42470EDD-7B3E-4E31-AC4C-3DCC02FD2C87.jpeg.86ebad7f6e11e42ad27706ea281f07ce.jpegDC6650D3-6FAF-4D30-BA8E-35C320DA670E.jpeg.23832340e12c2bb3494e423e1997551a.jpeg

     

    it was a lot harder than I thought. Took me all day. I couldn’t get enough length on the boom. (Thats’s what she...you know what) I had to remove everything off the front including bumper, grill, and even the hood mechanism. That still wasn’t enough. Had to modify the lift by drilling an extra hole. 
    203E98FE-63DE-47C6-BC2F-C5BA0397089A.jpeg.f556d7b3fbdf365ea37b89514abbddaa.jpeg6A3BD837-0410-47C8-A160-486C2BFE948D.jpeg.8542a31fbc69ab26a4f79b1908ee2674.jpeg

     Then I had a problem with the lift which was vapor locked. Had to take take it off mid install to cycle. Then the chains were hitting the firewall before I was even close to the mounts. Had to unhook everything and lengthen the chains so I could push it back. Very fiddly. I eventually had to undo the drivers side mount and bolt it back to the block after it was in. 
     

    I had to shave the top off that mount too since it was hitting the header. A small corner of the JCI mount also needed trimmed. 57D417EF-926F-49AE-9C9E-460150C92296.jpeg.032ca3d6515b841d19eed362a3bf6df8.jpeg
    the passenger side coil is very close to the battery tray. I think it’s going to be an issue later. 
    99C65023-68BC-4584-9750-EFB7237E9D37.jpeg.d812b855c620e18637a06f782c2ca240.jpeg
     

    had to trim a bracket off the passenger side for the header to fit. No big deal there. 
    331F9CC0-3FFA-48A0-960C-C08189C9133B.jpeg.8b26c95f3fb94b359c1623e5fd45f2b6.jpeg06DF86ED-1F20-4C14-AD15-15CF75A08BD2.jpeg.4064a015d063f0f10e0c55f8ff5aaf81.jpeg

  8. 22 hours ago, walkerbk said:

    Having done this before... do your self a favor and put the harness on the engine and get the general layout for how it will fit in the engine bay.


    thanks for the heads up. I’m going to wait to get it on the engine before i wrap it up. I have some new loom too. I’m going to try and get the fuse box, relays, and ecm in the passenger side. 

  9. I thought there were a lot of wires before. It’s pretty scary cutting all the wires out. LT1 Swap is the place to go. I also sent my ECM to Brandon to tune out VATS, emissions, etc. Easy peasy to work with. 
     

    I thought about just snipping the old stuff and not getting too deep in the harness. I’m glad I did. Was able to easily identify all the stand alone connections. 
    24BC5E04-8F3E-464D-817E-04CAE7415C98.jpeg.e4bd3d864a4604d05ed20c915a6fc8e7.jpeg
     

    here’s what I ended up with. Fingers are crossed. 
    0A5A363B-9575-4353-82AD-8500AC6CFFE0.jpeg.4178792e810669eb5a24a1998ef5ced3.jpeg
     

    hope I don’t need any of this! Wish I could go on a diet that easy. I’m not going to wrap it until it’s in the car-ish. In case I need to reconfigure anything. 
    4703AA2D-2127-47D3-958B-16F7218A8E43.jpeg.2bfbcf754509b3b54b3e2852f167c715.jpeg

    computer is back

    7DE9ABBA-BDAD-4324-8C41-2B36716EDCE4.jpeg.afc797972e118d2f77577209e6cbda00.jpeg

  10. bummer was really hoping for a yes that is normal answer! 
     

    Here are some more measurements.  The transmission shaft sticks out about a 1/4 to 1/2”. The yoke is about 3 3/4” and the splines go all the way to the edge  


    I can’t math real gud but that leaves about 2 1/2” of spline contact. 
     

    My gap is 1 1/2” If the normal gap is 3/4” would it be worth redoing the shaft to add 3/4” more contact? 

     

    5A8DFBD3-515C-44DD-A850-B6F918E5607D.jpeg.ae18cf0a8e34cd951bb59bdb52ba9ca7.jpeg

    1E34A057-CF1A-4201-9FCE-F8E3F624842E.jpeg.ba850ebc5dd109d31bd4a0f0bee36526.jpeg189A2471-E480-4410-BF95-CA2BF437189A.jpeg.66c763424afd933c0f8e33a8fc9fd2c2.jpeg

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