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Tony D

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Posts posted by Tony D

  1. Yes, the key is in the root of the female threads (and of the roots in the male thread going in!)

     

    If they are not completely clean... I mean with alcohol or chlorinated solvents so bare, dry metal is available, a 'leak path' can develop.

     

    Oil will sit down in there. If you have a burr on the peak of a thread that grinds through the root in the female thread it makes leak paths.

     

    In some cases I've used fine lapping compound to lightly 'work in' a fitting and take off nibs, nicks, and burrs with a swiss file before assembly.

     

    If you can get the proper Loctite Primer, it makes a GREAT cleaner and final-prep for the stuff.

     

    I will apply it to the male pipe threads after priming (and priming the female threads as well) and put my finger over the gob on the pipe to make a nice, smooth surface equal to the peaks of the threads. This pushes the sealant 100% into the roots and you can feel anything on the peaks that may cause problems.

     

    It doesn't need to be on thickly, pushed in making 100% root contact on the male threads, I will turn it in a few turns, then back out just a bit (kind of like tapping a hole) to insure the sealant is transferred completely between the first few threads on the female hole all the way to the root. I may go all the way in finger-tight quickly remove it all the way, re-smooth the surface, and then back in finger tight and 1/2-2 turns more.

     

    I find that working it slightly back and forth to 'work in' the sealant while finger-tightening seems to have a good effect.

     

    Once you put a wrench to it---DON'T BACK IT OFF! Carefully turn it to where it needs to be and STOP. I sometimes wipe the round bead that forms around the base of the male part...other times I don't touch it until days later to make sure the anaerobic action has worked from the bottom all the way to the top.

     

    I picked a lot of this up working on hot aircraft hydraulic systems. 165F and 6000psi tends to find leak paths on NPT. That's why they went to an MS-Straight thread O-Ring seal fitting design (which also allows for positionable fittings!)

     

    Ideally, the fittings on the end, if going to be adapted to an A/N fitting should really be an MS-Straight. Much more reliable in terms of leaks, and ease of positioning for various configurations.

     

    I digress...tongue.gif

     

    Good Luck in the morning!

  2. 53+25=78...

     

    Then again, service replacement blocks were shipped without serial numbers just "L24" "L26" or "L28"

     

    What difference does it make, really? Morbid curiosity?

     

    What is the number on the pad on the starter side of the engine>right after "L28"? Or is there anything there?

  3. Yes, we discussed this amongst ourselves---the reverse flow setup may allow for the lower flow of the EWP to function under full load. This would make both JeffP and I very happy (as others I'm sure!)

     

    My experience with reverse flowing a 600HP 6.6 Pontiac back in the 70's was that the flow requirement was considerably reduced. I didn't know why then, but in subsequent education later in life I realized the flow path on an engine is exactly opposite of any proper heat exchanger! RARELY will there be anything BUT a counterflow arrangement (lowest temperature coolant coming into hottest part of exchanger first). For this reason, I believe the stock pumps have to be oversized, as well as sized to pump to higher pressures internally in the block to suppress the obvious issues with steam pocket formation and cavitation in the liners and heads which can occur from steam impingement.

     

    We just ran out of time, and never got to the next experimental R&D session. As we were successful with stabilizing oil temperatures at or below 240F during these runs (WITHOUT EXTERNAL OIL COOLER) we were confident that the coolant system was adequate for the job, and wouldn't cause long-term problems. But being able to clean up the front end, and go electric for the possible post-cooling benefits still lurk in both our minds!

     

    Keep us posted on your tests.

     

    The oil jets, of course, would make another interesting thing to check on the dyno after knowing this engine had stable temps at 450HP under load after 5 minutes. Installing them on a known 'stable oil temperature' example would give a number that could quickly be calculated to determine what kind of BTU load these items produce.

     

    It would almost be worth it (if there was the time) to do this to a bone-stock L28ET and run the tests! Like JeffP says "Every time you start talking, it costs me $2,000!" biggrin.gif Curiosity killed the cat, but satisfaction brought him back!tongue.gif

  4. I kind of agree with Ray. The reason I bought a 260 was they are cheap, have better electricals than a 73 240, and all in all have better performance. I've accumulated 3 more to replace the one I have if something should go wrong---two were GIVEN to me as complete, running cars. A little rougher than the one I'm driving, but straight and complete. The other as I mentioned was $500.

     

    It's a relatively easy fix, just drive it till it dies. The parts may work out for you, but then you have a rotting hulk taking up space in your yard. Unless you have buyers lined up waiting for parts (I will give you $150 + shipping for your entire induction/exhaust system, orange air cleaner, flat tops intake manifold, exhaust manifold and headpipe .)

     

    But a 2.6 engine? Everybody wants L28's.

     

    A four speed? Need I say more.

     

    Interior? Good Luck!

     

    You're out less hassle fixing it and driving it than trying to sell it and replace it.

     

    As to this:

    "I was driving home from work after a 12 hour valet shift in the hot Florida sun."

    Come with me to Thailand's Interior, 50C and 98% R/H in the sun, climbing up and down on hot machinery and swinging like a monkey from scaffolding pipes to get around a piece of equipment because it was all set up for people 5' 2" and not 6'! I'm not having sympathy for that 'hard work as a valet'... sorry!huh.gif

  5. Core Charge is only "huge" if you don't support the vendor by returning the core!<br><br>I walk in, give them my crap part, and walk out with the new remanufactured part. No core 'charge' is ever mentioned or charged!<br><br>If you know the part is bad, drive to MSA (takes 45 minutes from Temecula, depending on which route you take) and exchange it for a reman unit.<br><br>No $400 Core Charge will ever come into the picture.

     

    <div><br></div><div>-- EDIT -- Customers would complain our core charges were 'excessive' as well---something on the line of $16K for a $16K part. The philosophy was simple: if you did't get the part back to us within 90 days, you were billed for it. It sure helped deadbeat and otherwise unmotivated lumps get off their butt and HONOR the sales contract they entered into: we give you a part, no questions asked, but we need your old one back! If you want the system to work, you gotta hold up YOUR end of it! -- EDIT --</div>

  6. Nissan Navara = Nissan Frontier

     

    Love that Turf Shot! PRICELESS!

     

    Maybe time to put up some 2m tall 30cm diameter concrete-filled pipe-posts sunk so only 'axle height' nubs stick up to defend your property!

     

    Make it look castellated!biggrin.gif

  7. Yep, I'm with Randy--idle in the 1000 to 1100 range if they allow it with the minimum timing you can get to run smoothly, then adjust for 'lean best'...

     

    A 1973 240Z adjusted in that matter using 72 Round Tops and AIR into one collector tube of the header (no EGR) piped clean to 83 Catalyzed standards!

  8. "but there is advantage to get a constant flow without cavitation"

    Not really, the variable flow from the stock pump is due to variable heat input. More rpms, more BTU's into the heat rejection system.

    IF the pump were capable of MAXIMUM EQUIVALENT flow rates, and you PWM trimmed it down I would say they had something there. But even with constant low flow, there is the possibility of cavitation. JeffP found the EWP was not up to it when pressed at higher HP for continuous use.

    Remember, we had his engine on the engine dyno and were running 5 minute pulls at power to see if all temperatures were stable. With the EWP the coolant (even on the dyno) temperature kept climbing. When we went back to the Diesel pump, the temperature stopped doing that--indicating to us at least that the increased flow rate given by the stock water pump was justified.

    These things usually work out in limited duration events, and on lower horsepower engines simply because the flow requirements are not that severe. When pressed, they seemed to fall short.

    All that being said, it MAY be different on reverse flow, the efficiency gained by doing a proper cool to hot reverse flow of the heat source may decrease the flow requirement to within the range of the EWP to handle it. 5 Minutes at max power on an engine dyno will tell you.

    Remember the photos on the cooling thread of Jeff's engine on there with the hose sucked closed???? Yeah, 5 minutes at 6300 and 450HP on CAST PISTONS and STEADY OIL/WATER temperature with the stock water pump (diesel)... Most guys don't run their engines for 30 seconds much less a minute at that level...but OEM's do. And you know Jeff, it's gotta be as good as an OEM or it's not good enough!tongue.gif

  9. "So it should probably have an N42 or N47 head, correct?"

    To paraphrase Shep Proudfoot from "Fargo": "Don't know that, never said that, can't vouch for that!"

    It has what head it has. Why guess or try to state anything without knowing what Nissan Supplied?

  10. " Making sure that the rail isn't cracked would also be good, but I doubt that "30-40 ft/lbs" would cause that kind of damage."

    I would disagree! ESPECIALLY if it was lubed with teflon tape. TORQUE is the resistance to rotary motion read on your wrench. On a common fastener, 15% of that resistance is friction on threads, 75% under-head friction, and 10% stretch on the fastener providing clamping. Changing the thread or underhead frictional coefficient can radically overtension the stud leading to breakage. Something small like changing from a graphite based to Moly-Based thread lube can affect the tension by as much as 300%!

    On NPT threads, just about the ONLY thing you have to resist torque IS thread friction! And this is compounded by the wedge action of the thread formation. Putting teflon tape in there radically changes the makeup torque---especially as the torque rises, and the teflon gets a chance to extrude and let the threads 'slip'!

    Proper thread makeup is starting with a clean dry fitting and determining depth at finger tight (which is somewhat subjective, but reasonably controlled) and then to go anywhere from 1/2 to 2 turns more with the fitting.

    Thread condition (burnishing) and thread sealant used can RADICALLY change how far that thread will engage--and subsequently which 'wedge loading' you will have from the taper.

    There is a reason everybody is saying 'check the rail for cracks'! It's SO common that the threads are 'torqued' instead of 'turned in' that the fittings on alloy parts split!

    Put an inch-pound torque wrench on a 1/4npt fitting and screw it in using '1 turn from finger tight' DRY and watch what happens as you 'torque monitor' that fitting on the first, fifth, and 10th installation. Each of those would produce a leak-free seal on clean-dry threads (or should!)

    From that demonstration alone you will see the torque variance rules out torque as a valid way to measure if it's 'tight enough'.

    Now put teflon tape on a new fitting, and with a new hole, turn the threaded fastener in to the same series of torques you recorded on the first hole. By about #5 I'm betting your thread is 100% bottomed in the hole---even though it was 'tapped tight' and had an issue fitting to proper depth initially!

    Like I said, I have a demonstrator for this stuff doing Training in China. Thread sealants and anti-friction anti-gall devices work great IF you use the proper installation method.

    I would venture to guess that 30-40 ft-lbs on a teflon taped 1/2" NPT fitting is about 100 to 200% overtorqued! Meaning colossal overstresses and thread deformation occurs in the female threads.

    They make up and stay leak-free with incredibly low torques... In the long and short of it, the NPT fitting is really an 'ANGLE-TURN' fastener, like many engineered fasteners on cars today. It's just the education about that point is lacking.

  11. Stagnant water is not good, one thing people forget about the stock pump, it generates 40 psig (around 3 bar) inside the block when running under load.

    This increase in pressure assists in suppression of steam formation, when you remove a high flow pump and go with something slower, lower flow, even if in reverse, don't discount the loss of that pressure under load which formerly helped stop that formation.

     

    Most electric pumps I've seen haven't produced flows comparable to the stock pumps and were only suitable for limited-applications.

     

    They may fare better in reverse-flow due to increased efficiency, it is unknown until actual testing is done. It would be great to do an instrumented test run on an engine dyno where you can compare baselines before and after the cooling system modifications--especially the reverse-flow!

  12. " I'm driving the Z mostly outside of Paris in the country side where twisty roads are (with no traffic jam)."

    For out in his barn, my uncle preserves for me an old Z, of 40-odd years... To keep it as-new has been his spirit's dream!

    Sounds like you have to watch out for those Gleaming Alloy Air-Cars!

    If you go to France, run the 'Reverse Blitzkerig' Route through Belgium and Holland...and stop by to see the Hybrid Z's in Frank 280Z's old Cow Barn!tongue.gif

     

    Once you're there "You're close to everything"!

  13. Don't feel bad. When I did the examples the guys at our factory STILL didn't believe me. The next day I saw four guys with a 36" Stillson and a 2M snipe on it reefing in a 2" pipe to the body of our Main Oil Pump (no, that wouldn't POSSIBLY distort the pump body would it?) they were going for 'another turn' rather than letting it "loose" and allowing the sealant to do it's job!

     

    I felt a lot better after we contacted the Loctite Rep, who was 'local' in that he was the same ethnicity. When he did his demonstration and barely turned a 2" fitting 360 degrees from finger-tight there was palpable discontent. As a few field guys interrogated him, he stood firm and insisted that was enough. A roar went up through the crowd. Nobody could believe a fitting "so loose" could hold ANY pressure. I couldn't speak the language, but by body language alone I know this was the case. So quickly I grabbed a regulator and screwed it into another fitting on the base plate and started pumping air into the vessel.

     

    Less than 15 minutes from turning in the fitting, the big fitting held 5psi (this was a hot oil reservoir that never saw more than 1psi if that...)

     

    It's very common, the educational level about proper bolting and threaded connections out there is amazing. When YOU start getting blamed for leaks (and nobody else in the world has them...) you start looking closer and learning a LOT about how to correctly put fittings together!

     

    When I started in Hydraulics, it was ALL metal-on-metal sealing. You learned CLEANLINESS was #1, wrapping of the dreaded teflon tape properly was #2. When those first Anerobic Sealants came out widely, it was like a GODSEND! Suddenly fitting makeup was EASY! But that lead to shortcuts, and nobody trained 'the old ways'... There really is no substitute for the basics: a clean joint, and proper fitting makeup and tightening. You do that, and you will have a good leak-free joint. Once you master that technique, sealants only add a margin of insurance, and the ability to make up the joint with far less angular motion. Meaning it comes apart and goes back together easier when it's maintenance time.

     

    Hope you got the leak nailed. If the fitting is bottoming out, you can helicoil the NPT, use red loctite on the outside of the coil going into the fuel rail, and PST 567 on the Male Threads of your fuel fitting after giving the red some time to set up properly. You should then be able to remove and remake the fitting without worrying about pulling the coil out later on.

     

    But if it ain't leaking...no need to take it apart again, right!tongue.gif

  14. "guess I didn't check the end play and 'assumed' it was correct."

    Measure 3X, Assemble Once!

    I always check and lap the thrust bearings to where they need to be. Picked it up teething on VW Air Cooled Engines where you have to set the end play with shims on the flywheel and you do it on every one!

    At least you know why now. That is completely within the realm of believable happenings. We continually disassemble machines at my job where we see thrust bearings coked and overheated. Outside of an oiling issue (which normally wrecks the journals first) when we see journals fine and thrust faces all grunged up and damaged--we check the oil clearance an without fail someone skimped on the clearances.

    Generally ANY bearing requires 0.003" for proper oil flow through the surface. This is big enough to let a continual flow cool the surface, build a proper hydrodynamic wedge, and let small swarfs (like fuel soot in the oil or the odd bit of broken off varnish from the oiling gallery) pass easily through.

    Go even 0.001" smaller to the 0.002" range and you run the risk of running hot and making varnish (which closes it up further, meaning more heat, meaning more varnish, meaning less clearances and so on and so on and so on...)

    Going to 0.004" and you decrease oil pressure if you have a marginal pumping system, but watching the oil throwoff temperatures you see it drop by almost 15F! (We can do this for new Engineers to demonstrate what gearbox setup items are critical. We can change these on our machines in about two hours while on the test stand...) On our High Speed Pinions (54K rpm) you will routinely see 75C with 0.003", but 66C at 0.004", and 85-90C at 0.002"!!! This is on the 'active' thrust side... the inactive always runs cooler due to little or no load so we don't instrument it.

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