Just got back from a frustrating dyno session - just seems like it's been one dumb thing after another for the past couple of weeks - pretty much right after I scheduled the dyno session...First I had the dreaded coolant leak under the dash. Had to order replacement hoses and wait - just got it all back together last night and it still leaked, looks like probably the valve was leaking too. So I just pulled the heater hoses and capped the block outlets for now.
Got to the dyno this morning and my laptop wouldn't connect to the engine controller - spent ~20 minutes trying to debug, finally reinstalled the serial port drivers and restarted and it worked. During the second and third pulls, the serial port started flaking out again, and apparently caused the controller to stutter. Had to shut everything down and reboot, and then that problem went away. Fouth pull was then very strong and we attempted some fine tuning, but during the fifth pull it appeared that the boost controller thought I was overboosting and cut boost.
Oh, and a small fireball around the intake gasket. .
So at this point it appeared that possibly the intake/exhaust manifold gasket was suspect - it ran fine but I didn't want to push any farther today.
So, a lot of f-ing around and two good pulls...
So here it is...
694hp/ 633lb-ft torque at the wheels on a Dynojet 248C...
The main new things on the car were:
GT4294R with a Mamba billet extended tip compressor wheel
a new proper Weldon 2025A pump
Three holley hydramat pickups plumbed in parallel
MOAR BOOST!!! 35PSI on E85
My son took some videos, I'll try to get a link up on youtube shortly...
Despite all the hassles, I'm pretty happy with the results!