after suffering a pilot bushing failure, a crossover pipe mishap, a manifold stud removal exercise, some mild head porting and full valve train re-lap and cleanup, and a turbo rebuild and complete (almost) engine detailing and a heck of a lot of paint, brand new bolts and fasteners from nissan, and some other tidy-up replacement garbage... she's almost back together.
Drove her for 10 days and had the pilot bearing rub against the input shaft violently, and it got chewed up.
I hate working on this engine while it's still in the car. If it acts up again, I'm pulling it completely.
Intake seating mockup. Injector seals on order. Goes on first before intake.
port almost finished. little bit of oil on the valve seat to stop oxidation
heads cleaned, assembled, and resurfaced (little bit of lint from packaging towels).
Intake detail. an hour a day of painting to get things right took most of the time while waiting for nissan parts.