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toolman

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Posts posted by toolman

  1.  Richard is absolutely correct you must prime the car quick as possible to  prevent flash rust.   I purchased 5 gallons of Hold Tight  for $200 to

    provide a 72 hours window before epoxy priming.   This solution can be mixed with media in wet media blasting or used with a 2000PSI pressure

    washer after dry media blasting.   It removes the salt and other contaminants off the metal into the air.   Bridges and metal building  even use Hold Tight prior to painting.

    1458534223_IMG_3456(1).thumb.JPG.17e3b5a239eb66b6a58239a42e49d73a.JPG

     

    Also, prior to epoxy priming, I spray Ospho-rust inhibitor around overlapping metal patches.   This is slow down any corrosion caused by the

    welding process.

    IMG_3431.thumb.JPG.44f7b54789623dcc6bdf007e6bf61ff1.JPG

     

    The vehicle was given another check for any rust that might have been missed.   If rust was found. the area was spot blastedIMG_3441.thumb.JPG.a928d3865c3118f2c3d03d95a31177ef.JPG

    A 1000 lumen LED portable light was utilized to find any missed areas( like cowl and other boxed sections)

     

    Epoxy priming was very difficult because of the enclosed and tight body sections( especially by the spare tire well).

    704529318_IMG_3445(1).thumb.JPG.d127bd7334a1cebdd7fee227430f0921.JPGBottom  view 

    IMG_3446.thumb.JPG.476272723fc52231f4a8eb77eea2d04b.JPG

    Front bottom view

    IMG_3447.thumb.JPG.2b490471971d52a57a495695a81e735c.JPG

    Front top view

    665589639_IMG_3449(1).thumb.JPG.7733fa4df0714797343ea86f49d3fc50.JPG

    View of the interior

    I sprayed  a gallon of white epoxy primer( costs about $200 with  activator).   Still have to touch up several areas for complete coverage.

     

     

     

     

     

     

  2. Rented a Ford F350 with 14 foot flat bed for $120/a day.   The sand blasting shop was on the other side of the island about an hour drive away.

    IMG_3421.thumb.JPG.f4f0a0d2f00691dc47922da940fb0233.JPGAt the sand blaster

    Forklifted into the blasting room

    IMG_3422.thumb.JPG.bf40aa46270f4b1c971e0489e7ad7d20.JPG

     

    View of blasting( lots of noise from the air compressor and very difficult to see anything)

    IMG_3423.thumb.JPG.6f039b7d60fc29e5b21df4ff170ee81f.JPG

     

    IMG_3427.thumb.JPG.6ab424d436ac6c15bc7136459ba58993.JPG  Almost finished blasting

     

    IMG_3429.thumb.JPG.852d4250da2daeac1891df7c36c475ba.JPG

     

    The 240z finally back at home.   Probably take a week to get most of the blasting media out of all those box sections.   Next step is seam 

    sealing the car.   This is another labor intense job that may take a couple of weeks.

     

  3. I made an appointment to media blast my z this Saturday.   Rented a Ford F350 with 15 foot flatbed and lift gate for $130 per day.   Unbolted

    the four 3" casters on the rotisserie and tack welded them to the frame rails.

    IMG_3404.thumb.JPG.b35ca5d182df22dc2da084da2e3589f6.JPG

     

    Side view of casters

    IMG_3405.thumb.JPG.aafdf8192b99ea5a87d4b3d97dea7d50.JPG

     The casters were transferred to allow easy movement of car to the rented flatbed truck.   With help from my neighbor and the liftgate, the

    move should be relatively easy.

    IMG_3409.thumb.JPG.05d86069685456b5a55d9b57e1da70b6.JPG

    Hard to believe, it took 15 months to get it this far!!

  4. This is the bottom view of the replacement hatch panel.  It was mocked on and the outer edge was traced with a black marker pen.  The area 

    below the line will grind with a 50 grit sander.   Existing rear panel matching area was sanded.  Adhesive must thoroughly cover all grinded areas.

    IMG_3376.thumb.JPG.e948743a73cf601c3f6495a409c894f3.JPG

     

    The Lord Fusor metal to metal structural adhesive was used to bond the replacement top panel to the existing rear panel.

    IMG_3378.thumb.JPG.4a42b60b0926c8f7e40e276f3f37b14c.JPG

     

    The panel is installed and bonded.  A dozen vise grips are utilized to hold the panels together until curing is done(in this case about 8 hours).

    IMG_3375.thumb.JPG.84fd2770b2bc3394d95bdc6cb0216281.JPG

    Note-the vise grips are all numbered with corresponding numbers on tape located on the panel.  These adhesives usually have a fast setup time

    so preadjusting the vise grips was done.

     

    The next day the vise grips and excess adhesive was removed from the edges.

    IMG_3383.thumb.JPG.3a1048c1d78ffbe0ae413bce02c68819.JPG

    All the seams will be sealed after epoxy priming.

    IMG_3384.thumb.JPG.35a3c4d4d348dbbc942d7ef4a75c1d1d.JPG

    The Lord Fusor structural adhesive costs about $50 and special applicator gun runs about $50 too.  This adhesive is OEM approved

    products and even crash tested.

    This post was rather long so let me know and I try to keep posts shorter.

     

     

     

     

     

  5. I had planned to wet media blast the car this weekend.   Unfortunately my 3000PSI gas powered pressure washer didn't cooperate.

    Took a day to get it running which screwed up my time frame.   This is because after wet media blasting, there is a 72 hour time limit to

    epoxy paint the car before corrosion sets in.    With a 24 hour drying time, there is not too much time for error.   Also, the weather also

    has to cooperate too.    So I decided to put blasting on hold until  the next weather window opens up.   Instead did some welding inside of rear

    hatch panel.

    IMG_3361.thumb.JPG.e7b144e3b10d7fce1089562365a43e7b.JPGRight rear hatch panel-inside view

    IMG_3363.thumb.JPG.6bb2b3e9eb6b85c5fe5662e3966c29f9.JPGCenter of Rear Hatch Panel-inside view

    IMG_3366.thumb.JPG.e88b713c08b69077f28c65256d6011b6.JPG

    Left Rear Hatch Panel- view from inside

    IMG_3369.thumb.JPG.f6ffb6ce30981f3fe05477cb53ce70eb.JPG

    Overall Top view of Hatch Panel.    I decided to use a different method of attaching the top replacement hatch panel.   The new replacement

    panel is even constructed of 20 gauge metal.  I have not seen a 240Z that didn't have some corrosion under this panel.   So I decided to use a metal to metal automotive epoxy to hold this panel on.   The epoxy will also seal the panel from water getting  under it and rusting.

  6. While cleaning the cowl area, I discovered another rust spot[hopefully the last one) in the extreme left side of the cowl.   Anyone who has the cowl panel off the car should check these area carefully for signs of corrosion.    Most people do not realize that majority of the rain water coming off the front of the roof enters the cowl area then drains down the door post pass the front fender.    Combined with dirt, leaves and other debris, corrosion begins.

    IMG_3341.thumb.JPG.66176e6de54a96739c386f60579ab891.JPG

    The rust is difficult to see (above half way down from top) on the upper edge of reinforcement plate.

     

    Pic of corrosion cut out-view from the interior side of cowl

    IMG_3339.thumb.JPG.c1072bfd622d8cbc2d539333dc695ea3.JPG

    Osho  was shot under the reinforcing plate to prevent further rust.   One edge of the patch was pushed under this plate then

    the patch was welded in from the cowl side.   But because the cowl support rib was blocking any work, the spot welds of the rib had to be drilled out.   It was still difficult to use the mig because of the confined space.  Of coarse, after epoxy priming, all seams and air ducts will sealed with urethane seam sealer.

     

     

     

    IMG_3346.JPGHidden corrosion repaired

  7. Spent most of the Holiday weekend, rewelding welds and patching small corrosion holes.   But managed to finish the inside fuel filler box and mount 

    it.  I used four 5/32" machine bolts to mount it to the quarter panel.   Their heads had to be grinded down to clear the filler door movement.

    IMG_3332.thumb.JPG.9c07a4d47dfb4f24fe5a3f4843913708.JPG

    Also, have to fab two small rubber snubbers to prevent contact when closing door.

    IMG_3333.thumb.JPG.b69b15290e36b06e525e4975c54a76b3.JPG

     

    Most of the Z has almost all of factory paint, primer and undercoating completely removed down to the bare metal.   Spray can primer was

    applied to prevent rust.  The whole car will wet media blasted then painted with epoxy primer,

    IMG_3290.thumb.JPG.6c13d799df6e5408927f453e0f9a5436.JPG

     

    IMG_3286.thumb.JPG.ae4e5e1b1b550b5545bd2ede6ca80444.JPG

     

    IMG_3287.thumb.JPG.022b84f797be286c42809c4a21fc14aa.JPG

  8. While cleaning up the blast media in the car,  I found a lot of rubbish and media stuck in the boxed sections of the Z.

    IMG_3330.thumb.JPG.fb98cff63badbbf6295163752d8792f9.JPGThis rubbish was in the upper frame tube alone.

     

    So I decided to drill 1/2" holes in those hard as access areas for two purposes: allow blast media to be removed after blasting.  Second: to

    allow rustproofing in those areas.

    IMG_3328.thumb.JPG.2177e30105508d8f1e8cc4428d021d25.JPG

    Rear quarter panel dog leg/ wheel housing area is not accessible  without this hole here.

    IMG_3326.thumb.JPG.53d2111e9cb2785f74575ff81723d873.JPGFront door post / upper frame tube area-eight access

    holes were drilled.

     

    IMG_3327.thumb.JPG.4c3c3becb80144e8dfdc881e712461a0.JPGUpper frame area

    IMG_3331.thumb.JPG.632d7347515ecd6dfc4780d1276a9198.JPGRocker panel area

    About 14- 1/2" access holes were drilled on each side of the car.   These holes will be capped with rust proofing plugs after wet media blasting and epoxy priming.

     

  9. While working on this Z, one problem that coming up was the presence of wax type of rustproofing.    Even when I tried to clear the rustproofing around the area of repair, it sometimes would melt and spoil my weld.   I tried scrapping and using lacquer thinner but it still was not effective.  One of body shop guys told to try Barbeque Lighter Fluid.   So I bought some from Walmart.  It was only $3 a quart.   Well. it works good as it does not evaporate as fast as lacquer thinner and allows time to soften the rustproofing.  A stiff parts brush also helps also.  The fluid doesn't seem to leave a residue too.  For areas with thick rustproofing,  use a plastic scraper to remove the heavier deposits first then use the fluid.

    IMG_3294.thumb.JPG.4f66e06ba662413df0649adf2fc8d50a.JPGPic of rustproofing on the inside of left quarter panel

    IMG_3293.thumb.JPG.26c315a7e72582394e156319f1e797d2.JPGLighter Fluid

    After cleaning with lighter fluid, the seams were scrapped out with thin scraper.  A 1000 degree heat gun was also used to soften the seam sealer.

    IMG_3296.thumb.JPG.82b4e9cc7099fd5cfa488a34a7ead448.JPGLeft rear quarter panel pocket 

     

    Right side pocket after cleaning.  Brushed on OSHO in the seams then neutralized it after 24 hours.

    752046720_IMG_3298(1).thumb.JPG.8b74627c3eec8822a0bcefbd93ef424e.JPG

    Lighter fluid seems it work well and allow me to remove the factory seam sealer in the panel.  Have not decided  on what type of rustproofing to use after painting though.

     

  10.  

     

    The contour of the inner edge was time consuming.  Utilizing a large c-clamp and pieces of 1/4" steel plate to make a temporary screw press.

    As you can  see, the method is very effective and very low cost.

    IMG_3263.thumb.JPG.8b21d3021b625c5c5e7ad650e050fe29.JPG

    Guide lines and position marks are very important  for correct alignment.

    IMG_3262.thumb.JPG.2b1eba03e7a1356149b35e5a65108721.JPG

    The patch was ducted taped to the quarter panel and fuel filler was test fitted before welded on.

     

    The patch was welded on and painted with welding primer.

     

     

     

     

     

    IMG_3279.thumb.JPG.307d88c1754ace892ee1dcffea2df579.JPG

     

    The fuel filler door  was doubled checked on the exterior patch.

    IMG_3278.thumb.JPG.83075c5a5598890613f8ccdb1862a97e.JPG

     

    The exterior patch was also tack welded from the inside.  It will be seam sealed after media blasting to prevent corrosion.

    IMG_3280.thumb.JPG.2f4fd2c36bdad2c9aa3f28f599296569.JPG

     

  11. While waiting for the replacement dog leg panel to arrive,  I decided to add an additional drain hole in rear area of the inner rocker panel.

    A corresponding hole will added to the replacement panel which goes over the rocker panel.

    IMG_3234.thumb.JPG.0c5ce8d808ee04ec80781e50cda2847e.JPG Also, as the wheel housing side will be open till flaring

    I will spray seam sealer to protect this area from corrosion.

    IMG_3232.thumb.JPG.4ff707389a03e3fe55ddb1143b9c889d.JPGReplacement panel ready to be welded on.

    IMG_3251.thumb.JPG.58c666cf8bdc1b3abe16a67b8d25f748.JPG

     

    I found additional corrosion on the bottom front edge of the fuel filler door area.IMG_3237.thumb.JPG.44d7a3f63027f9e427e9e2f713816df5.JPG

    Additional corrosion was discovered on the innerbox section too.

     

    A template was made to create a sheet metal patch.

    IMG_3246.thumb.JPG.98a62817201d3e212693fe9b1bf0daee.JPG

     

    This photo shows the inner fuel filler box corrosion.

    IMG_3239.thumb.JPG.406c79fe43021d4398ec2260bf4c8e11.JPG

     

    The replacement section had to hammer formed to match the original.

    IMG_3242.thumb.JPG.bd0f0cdd24d3b8ea4736ce42c8872237.JPG

    IMG_3247.thumb.JPG.37e2c80fac0a8867e913725b5f5a748c.JPG

    The exterior replacement panel  being mocked up before shaping work.

  12. I found similar corrosion  on the right side door dogleg.   Had remove more of this side rocker panel due to rust.

    IMG_3212.thumb.JPG.7d39f89fafa292c70958d3d858c0d0b3.JPG

    The wheel housing also had to patched.  In my opinion, this type of wax type of rustproofing was not thin enough to get in those tight cervices and pockets.   

    IMG_3214.thumb.JPG.9009e0e879f01250e9818a0fc20d4594.JPG

    Also, the use of weldable primer will help to prevent corrosion from the mig welding process.

     

    The pictures show the sections of patches for this repair.  Only the upper left section is left over from the original rocker panel.  The other

    three parts will be fitted together like a puzzle.

    IMG_3215.thumb.JPG.168fe74d5e86e4307fa4ec0c7399fcfc.JPG

    A different view of the patch sections to give a better idea of the different sections.

    IMG_3218.thumb.JPG.7dbc5b771bcd67d290be88c77e17e4ff.JPG

     

    Utilized 20 gauge metal for the wheel housing patch to resist corrosion.

    IMG_3226.thumb.JPG.eea24ec3d69da5e4585dc1fc19bd06d5.JPG

    Marking a template for the curved section of dogleg.   This is the second patch for this section because I had cut the upper potion of the original

    curved section to allow welding of the rocker panel.   Also, still have do more welding of patches.   Waiting for the replacement corner section of the dog leg

    from Z Depot which cost almost $100 because of freight.  We call it the "Paradise Tax".

     

  13. This is a photo of the left side of the rear hatch panel after media blasting.

    5ae6c8b865275_IMG_3177(1).thumb.JPG.2454d48727135e86ca55f2286a8f3022.JPG

     

    Made template for patch for left side.

    5ae6c970794b7_IMG_3179(1).thumb.JPG.00a1830bc7b703d02b1347faf7d05158.JPG

     

    IMG_3180.thumb.JPG.36ebc4a742193f9b02eb744754d24535.JPGRight side template

     

    Had to even to use a Dremel to hard to cut tight areas.

    IMG_3186.thumb.JPG.ba16e93627f5f531e9f73048d292d52f.JPG

     

    Right side dog leg section finished.  I utilized a gas torch and butt welded the joints to provide a smoother finish.

    IMG_3190.thumb.JPG.3e88e4d4888decd46c7277ac5f0a26d8.JPG

     

    5ae6cc9797865_IMG_3184(1).thumb.JPG.41a620959d9ea7f4292824806316fce1.JPG

    Left lower section finished.

    Still working on the horizontal panel between both quarter panels.

    IMG_3173.thumb.JPG.290f17d301d67f743c98a89e3fad86b5.JPG\

     

    Also, repaired this hole by butt welding with gas torch with 1/16 steel rod.

    5ae7fe3e41428_IMG_3193(1).thumb.JPG.4164bdb743cbe75408fcf916632e851f.JPG

     

    IMG_3205.thumb.JPG.9a0f01f9923c3f30e864fdad57a1c889.JPG

    Butt welding provides a finished surface requiring very little body filler.   With a Tig welder, you can get away sometimes with no filler at all.   But the patch must close fitting thus time consuming.

     

     

  14. Today was the first day that my Z was turned around in the garage.   It has been over 1 year since the restoration started.   During that time,

    I was looking for another 240z or even a parts car.   Because of our high humidity and being surrounded by saltwater,  the 240Zs that I looked at

    were real "rust buckets".   Only consolation that I have is that nobody here (that I know of) has went through such a complete restoration.IMG_3141.thumb.JPG.28fd46cc3c78b6f2cbae25c87f400f75.JPG

    The Z finally turned around in my garage.

    IMG_3142.thumb.JPG.50bbf79a4e357f91da3cf3b072eba02d.JPG

    Only the right side of roof, rear panel and right quarter  left to strip the paint off.

    IMG_3139.thumb.JPG.976aa6722e2d93d3e23bf775a770067f.JPG

    Managed to finished the upper left quarter panel patch.IMG_3135.thumb.JPG.411b519fa9941411816c4802ad21594c.JPG

    The dip rail was made of 20 gauge metal.  urethane seam seal will seal the drip rail after epoxy priming the whole car.IMG_3136.thumb.JPG.093854e066134ec07c714651c5d8f29b.JPGBottom view of patch

     

    IMG_3138.thumb.JPG.52baa810489b5d8851f44b7cf6106b35.JPG

    Interior view of patch

    IMG_3126.thumb.JPG.e87781ba5dde1e2fced9f2ca684d2120.JPG

    For extra protection, I used a 1/2" Blair hole saw to drill rust proofing access holes.  A bendable magnet is used to recover the drilled out piece.  The 1/2" plastic plug will seal the hole after rust proofing treatment is done.

    IMG_3124.thumb.JPG.8e505acf3493cf4b981a97602cb8d85a.JPG

       The rustproofing hole is just forwarded of the repaired area.   Also, it will allow rust proofing of the hatch hinge area(another corrosion point).   More access holes will drilled in potential corrosion areas through out the car.  Rust proofing will performed only after final color painting .

       Thanks again for your praise.   Most people do not realize how much work there is for 47 year old vehicle restoration.

  15.   This weekend. I started on the corrosion on the upper section of the right quarter panel.

    5add7287a1b7f_IMG_3099(1).thumb.JPG.3c74185baee0e0cbafedbeb2eea772e0.JPG

    This area was little heavier gauge(about 20 gauge) but had to be removed.

    IMG_3098.thumb.JPG.5e2ce36594588402c9f47d9a09388332.JPG

    The removed area, in this case, was about 5".

     

      Just the left of the front cut is the connecting area of the quarter panel and the roof.   This joint was welded then lead soldered at the factory.IMG_3120.thumb.JPG.3827723d2f42eb906c3039e76144fdcc.JPGAll of the lead solder must be removed before work

    can be done.  When this car was manufactured, using lead for the roof joints was common practice( even on US made cars).

     

     A template was made to provide reference points when reconstructing this area.  In this case, the template was copied from the opposite (right

    side) and image reversed.

    IMG_3100.thumb.JPG.dc767306eca3dc576a50205b74f135d4.JPG

     

    The drip rail patch was constructed using several paper templates.

    IMG_3115.thumb.JPG.3267ea0b238b3aef304db8433608eed3.JPG

    Note: both front and rear ends of the patch have extra material to allow welding to original metal.

    IMG_3116.thumb.JPG.45cd1796c929073db660c9d79e8171ed.JPG

    If you notice that I marked directions on my work,  it is because it is easy to get confused and place the patch the wrong way.

     

    The lower portion of the patch welded the body.

    5add7eeccc03b_IMG_3104(1).thumb.JPG.41441ad5a29c1383ca17e7f77a304c37.JPGNote: The drip rail is made taller and will be grinded down after everything is completed.

    IMG_3122.thumb.JPG.19d826d567d3fde32f23c00a3885a536.JPG

    The seams in the interior of the patched area were tack welded to increase strength.  Then painted with welding primer.

     

     

     

     

     

     

     

  16.   I almost made a mistake.   When I was watching a video of 240z replacement of its rocker panel, I realized that my rocker panel had to be longer.  So I constructed a new longer rocker panel  section.  This is a photo of what I can up with.

    IMG_3076.thumb.JPG.87433057d2fcf1a756f16ddff63b9a62.JPGBasically it is just longer than the old one.

     

    But the new rocker also had to be "capped" at the rear.

    IMG_3079.thumb.JPG.d69d2ba37f9737d7326a67e11b8784bf.JPG

     Interior view of the new rocker panel.

    IMG_3082.thumb.JPG.ad195bf6d11a08759bccee7fab56eabe.JPG

    This pics shows  the rocker panel welded in place.

    IMG_3084.thumb.JPG.36e1547147b706993d4a43b8cf6ecced.JPG

    Now, templates were made to construct front upper and side step for the dog leg.  This required  three separate metal pieces to make this complex shape.

    IMG_3085.thumb.JPG.cf9b089ffbc4060d4b0707dc69c1db00.JPG

    Used a oxygen/acetylene torch with 1/16" steel rod as the metal was so thin.

    IMG_3086.thumb.JPG.5b60380e3044b82ca0dc7b9025805011.JPG

     The finished front upper section of the door leg( three separate pieces of sheet metal welded together).

    IMG_3087.thumb.JPG.13569862d370d83b5cd556a9adc9db46.JPG

    The welded section was then welded to original dog leg and then painted with welding primer.

     

  17. After waiting for my replacement dog leg panel for a month, I canceled my order with them.   I then ordered the panel from Z Depot instead.  It

    came in one week.   Now I can finished up the corrosion repair.   I welded in the inner reinforcement panel and painted with welding

    primer.

    IMG_3059.thumb.JPG.505de9148942531610c23b679a0177f4.JPG

    Now to fabricating the upper portion of the dog leg.

    IMG_3038.thumb.JPG.c293b9e8629459b949b386d2d2275e1d.JPGFirst , a template must be made .

    Using a metal shrinker , the upper dog leg portion is created.

    IMG_3039.thumb.JPG.fd3cea46807b8214620b2a6957c985c6.JPG

    With the upper portion mocked in, the next lower stepped area can made.   The picture below shows the dog leg and this stepped area

    together.

    IMG_3057.thumb.JPG.8c116ca95aba2b3a996d80cdde6d3d89.JPG

    Next, the gap between the rocker panel and the dog leg must be filled.  Another template  for this gap is made.

    IMG_3048.thumb.JPG.da7552a2e4c91add070e7d5d384c3672.JPG

    There is six separate bends that required.   Even with a template, mistakes can happen.  Just straighten it out and rebend it.

    IMG_3049.thumb.JPG.84f8aa12c4085b13cbb4780400c4257e.JPG

    Sometimes even with metal brake, you have to use "red neck" technology to get the job done.

    IMG_3051.thumb.JPG.ae06ded61fb4fdc96d0807c5f717aca3.JPG

    Almost finished, the patch and dog leg ready to be welded.   The wheel opening end won't be welded yet as the new flare size has yet to be determined.

    IMG_3053.thumb.JPG.a3f321bd0c3ecd8b6925c28254599353.JPG

  18.     After  rotating the car to the horizontal position,  I attached the two caster cross members.   Pushing the car around was fine but I noticed that

    the rotisserie was wobbly when moved.   So I decided to  add a 1 1/4" galvanized conduit between the two ends of rotisserie to solve the problem.IMG_3030.thumb.JPG.8fde05f9287954739f2de0196cc9aea7.JPG

     

    Two mounts were made to hold the  15 feet of 1 1/4" conduit.    Two 5/16" x 1" lag screws held the mount to the cross member.IMG_3031.thumb.JPG.f0c867b4ad0e1e00830693a05ecf3681.JPGA 3/8" bolt with welded nut holds the conduit in place.

  19. The quarter panel dog leg section is still on back order from the manufacturer so I just do other body work for now.   Next, the old metal reat fender flares must be cut out with aIMG_2994.thumb.JPG.8f29979989272f975812f12244cba317.JPGcutoff wheel and air saw.

    Additional flaring work must wait till the new wheel and tire configuration is determined.

     

     Inside view of cut out fender flare

    IMG_2991.thumb.JPG.eb8ebe622207f9b74e8a86aee5265703.JPG

     

     

    The left rear quarter panel was stripped of previous paint jobs (about three) plus the original primer and color.

    IMG_3011.thumb.JPG.65ef8216d1c5fd25ecbb812996f88242.JPG

     

    To aid in paint stripping, the addition paint layers( besides factory ones) can be removed with a single edge razor.   In this case, the top 3 paint layers came off in one'

    thick piece leaving only factory color and primer left behind.

    IMG_2999.thumb.JPG.c3d454ea30bf5152da043870c6dd0ac4.JPG

     

    Since  I had some extra time, I decided to add additional lights to my garage area.   Two 4000 lumens Led Shop Lights on Amazon for only $30 each were installed.

    IMG_2984.thumb.JPG.11f7118c1e591a2c89cc38f857da4b6a.JPG

    As you can see the two LED lights really brightened up the garage.  I will probably add a couple more to light the sides of the car when I am painting.IMG_2982.thumb.JPG.0c55f17fdf1e5782a004f0892cff4fbd.JPG

    IMG_2982.JPG

  20. Returning to  Low Cost Rotisserie topic after almost a year.   Preparing my Z for media blasting. I decided to work on the rotisserie.  As the car will probably be in the normal upright position for the most of the rest of the restoration, casters must be added to provide easy movement.    Utilizing two 2" x 2" x 1/8" right angle shelving brackets formed into "U" shaped channel support between the two vertical supports of the rotisserie. 

    IMG_2959.thumb.JPG.7bf669d9c651563c9d473dea52f7b90d.JPGTwo 4" metal casters were added to bottom of the channel.

    IMG_2961.thumb.JPG.c18c1193fbad4555f883b0c08fce4690.JPGSupport channel is about 88" in length.

    Each side of the channel us attaches to the rotisserie with six-5/16" x  1" lag screws on both sides.

    IMG_2962.thumb.JPG.29abff56b3ddda7b3204a079ba8fa8da.JPGBack view of front caster support channel.

     

    IMG_2966.thumb.JPG.80c25932c59f308216519dc7ef63714a.JPGEach 4" caster has a load rating of 250 lbs.

     

    IMG_2965.thumb.JPG.1052951db8dd1d977cdcbc9524507465.JPGPic of rear caster support channel

     

    These caster channels will be slid in position/ bolted down  after car is in the horiziontal postion and jacked off the ground.  These 4 swivel casters will allow the vehicle to be turned completely around  with ease.   Cost of casters was $10 each-Home Depot and shelving brackets were free(dumpster diving)

    IMG_2971.thumb.JPG.ee78e955f775b2a50d04e0ccdbfbe241.JPG

    A 2" X 4" board was cut down to fit in the center of the support bar and bolted to frame with  four 5/16" x  2" lag screws.   This was to provide additional strength when floor jacking on the bar.

     

     

     

     

     

     

    '

    IMG_2970.JPG

    Overall view of addition to support bar

  21. Returned Sunday from a convention in Las Vegas but managed squeeze  three hours of Z work time in.   As I was waiting for the front 

    lower quarter panel leg, I decided to pull out two dents on the same rocker panel.

    IMG_2922.thumb.JPG.88ca7235eb6a65dc2af89a06e6f5a10e.JPGTo do this, a 110vt stud gun was utilized.

    The gun spot welds copper studs to the damaged area then the sliding grabs and pulls the dent out.

     

    Pic of crease  on rocker panel.

    IMG_2927.thumb.JPG.faf6c56f089a3696fd0aa930f365cb9d.JPG

     

    Another angle of stud pulling.

     

    IMG_2934.thumb.JPG.2a72cac32e3fec8554a6b821afa92dcf.JPG

    If the repaired becomes "high" ,  there is also a shrinking tip that can be used.   This flat tip will heat a small area "red 

    hot" then tap this area with a body hammer down.   Next, "quench" the area with a wet rag. This will create the shrinking action to occur and lower the area.

    IMG_2937.thumb.JPG.871bab8a45c1a9a091fb4792f9c10251.JPGRepaired area after grinding with#24 grit paper

     

    IMG_2939.thumb.JPG.d754ad20d2e4945b191dad2443369081.JPGPic of the other dent repaired with stud gun

     

     

     

     

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