We stoped the dyno run as soon as we noticed the misfire. I asume it was a slow blow that let a small amount of combusting gases past and into the next cyl untill there was enough loss in compression to cause a misfire.
I drove it home about 5-6 miles only with the injectors to 3/4 disconected.
Yes, this is what happens when the gasket material is burnt out from within the fire ring.
+1mm over
also it is meat to see fire on its inner most surface and to dissipate this heat with the other 2 faces.
14psi, did 309whp & 329ft/lb